Page 49 - ChipScale_Nov-Dec_2020-digital
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Fo r t h e p r o d u c t io n t e s t i ng , a   Summary            cleaning methods negatively affect UPH,
        dimensionless contact resistance ratio   Advanced processes, tooling, and   and consequently, increase the overall cost
        (CRES RATIO ) was defined and used to   practices are necessary to meet these   of test.
        assess the cleaning performance. The   industry and consumer expectations.   All major suppliers of roadmap
        CRES RATIO  is defined as the maximum   Reliable package-level testing is critical for   handlers have developed and incorporated
        resistance value (CRES MAX ) divided   meeting the requirements of KGD, KNB   programmable ACC functionalities.
        by the upper specification limit of   die, and “zero-defect” manufacturing   Programmed preventative cleaning using
        the resistance (CRES USL ). In a stable   without cost of test escalation. To maintain   the handler automation for “on-demand”
        testing process, the CRES RATIO  should   yields and consistently attain high data   cleaning execution dramatically improves
        have a value that is less than or equal   integrity, regular socket cleaning is   test cell OEE. Auto cleaning execution
        to 1.0. If the CRES RATIO  is greater than   needed. Reactive or proactive manual   is performed using customized cleaning
        1.0, the testing process is considered
        to be less than optimal with a high
        probability for additional recovery
        passes. During the qualification, the
        two types of cleaning units (flat and
        featured) were loaded simultaneously
        into different cleaning repository
        locations of the high-volume handler.
        This relatively simple evaluation
        strategy allowed for an iterative “on-
        off-on” comparison to validate the
        use of functional features for the
        process stability.
          I n t he test sequence, feat u red
        c l e a ni n g  u ni t s  w e r e  i ni t i a l l y
        i mple me nt e d a nd t he  CR ES R AT IO
        remained below 1.0 during the testing.
        After the first set of featured units were
        cycled through, a second set of flat units
        were used for the cleaning execution.
        As these cleaning units were cycled
        through the test cell, the trending for
        the CRES RATIO  values progressively
        increased with a greater variance
        (Figure 8). The f lat cleaning units
        can  remove  debris  from  the  surface
        socket f loor; however, because the
        crown tips of the spring pin protruded
        less than 90µm above the socket
        floor, these were not getting properly
        cleaned. Upon reimplementation of
        the featured units in the sequence, the
        CRES RATIO  incrementally recovered
        as the crown tips and the guide holes
        star ted getting properly cleaned.
        After several cleaning executions, the
        CRES RATIO  stability was reestablished.
        By creating the functional features,
        it was possible to control debris from
        within the floating base socket guide
        holes that could not be addressed with
        the flat, unfeatured units. The “on-off-                                                   RoHS
        on” sequences were performed several                                                      P
        times with practically identical results.
        At the conclusion of the project, it was
        clear that the featured cleaning units
        were significantly more effective for
        maintaining stable electrical contact
        integrity for the floating bed socket.


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